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AC3.4-RC5 Hard Landing - Loss of Altitude / Throttle Control

@wn0x wrote:

Appears to start at entry 542 in the log. Very fast descent with no throttle control in POSHOLD. RC IN on channel 3 appears to be at maximum. Roll/Pitch/Yaw responsive. Switched to stabilize to regain control during last minute of flight but still unable to increase altitude with maximum throttle. Auto analysis indicates motor imbalance but considering the very fast descent and loss of control I am not sure this is relevant. BARO.alt appears consistent with flight.

2016-10-18 18-12-45.bin (2.9 MB)

Pixhawk FC on 700mm spider quad, 6600mah 6s battery, Hobbywing 40a ESC, Foxtech 3508 380 KV motors. UAW about 3.4 KG.

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