@frizensami wrote:
Hey all, I've just recently flown a Goblin 500 Sport with Arducopter 3.4.4, and a few seconds after takeoff in Stabilize mode, it came straight back down and hit the ground hard even with close to max collective and fairly high throttle. I'm using a Hobbywing Platinum 100A V3 ESC in governor mode and have roughly 2000-2100 RPM headspeed. I can't conclude much from the logs except the throttle and collective values, perhaps someone else could take a second look?
2017-01-08 08-09-47.bin (1.3 MB)
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