@iseries wrote:
I was doing a test today to see how 3.5-rc1 flies.
Before takeoff copter had status 4 on GPS. Flight controller is a 3DR Pixhawk. Accelerometer, Compass and Radio calibration done before takeoff.
Took off in Stabilize mode and later switched to Position hold. Copter started to drift to the left. I repositioned it several times until it finally stop drifting. It held it position for several minutes in high winds of about 25-30 miles per hour.
Later I flew it forward and then back. After it flew back it suddenly flew to the right 50 meters. I let it go to see how far it would go. I finally flew it back and it again held it position.
Looked over the logs and did not see anything to explain the sudden change it position.
The sudden change occurred between 171000 and 181000.
Also there are leading zeros on the log file name, 00000354.bin, and the date and time were blank.
Mike
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