@Conny_Gyll wrote:
Hi!
I made my first successfull take off today. F550 hexacopter, ublox GPS and Devo7 transmitter. The hexa hoovered like no drone I ever flown before. Marvelous and beautiful! I flew a few meters and then let it self stabilize two-three meters above ground. Then the whole copter tilted and started flying away. I panicked and pushed "hold pos" but nothing happened for two seconds so I increased the panic and pressed "return to home" and two seconds later the whole thing made cartwheels over an old dusty road and collapsed in a heap of parts. (I think everything except two arms and the main board is salvagable)Can anyone help me with the log files and see what went wrong? The only thing I can decipher is DCM bad heading, and that dissapears after a few seconds. The copter drifting off and then bolting away into the road was (as far as I can tell) in direct opposite of remote commands.
Thanks in advance!
LOGS:
2016-06-06 20-54-03.tlog (152.7 KB)
Posts: 3
Participants: 2