Quantcast
Channel: ArduPilot Discourse - Latest topics
Viewing all articles
Browse latest Browse all 46108

Trolling motor noise?

$
0
0

Hi everyone, this is my trolling motor. I’ve been testing it for some time but I still can’t calibrate it for the various GPS-guided functions. Meanwhile, a brief description. I emptied the upper part and inserted the fc CC3D (in the front), the rc receiver, and two brushed esc behind it. in the upper part and far from the esc the compass with the gps. Logically, one ESC will turn the trolling motor and the other will turn the propeller. I have done all the calibrations and the steering seems to work well even in ACRO mode. The main problem concerns the loiter mode. Once set initially the steering works but when the propeller motor starts there is noticeable steering vibration and the motor loses course. As soon as I disarm the trottle everything moves perfectly. I imagine this is due to engine disturbances… However I ask if there is anything I can do or any advice. I’m attaching a video and a file if anyone wants to take a look. In the meantime, thank you. O my god, How do I attach the video file and the parameters of my FC???2024-06-19T22:00:00Z UTC

3 posts - 2 participants

Read full topic


Viewing all articles
Browse latest Browse all 46108

Trending Articles



<script src="https://jsc.adskeeper.com/r/s/rssing.com.1596347.js" async> </script>