@Hubertus_Paetow wrote:
Today after flying around in stabilize i switched to pos hold and contiued flight. after about a minute without any action the motors stopped and copter started falling. I pushed up throttle stick to the max and copter managed to stabilize again and i was able to land. Log shows nothing that could explain this behaviour, but you can clearly see the throttle drop.
Setup:
Frame: 3dr Y6b
Motors: Emax 3506 650KV
Props: T-Style 14 x 4.8
ESC: Afro slim 20A BLHELI-flashed
Batt: Multistar 10Ah 10c 4s
FC: PixLite with Neo M8N (Drotek), AC 3.4 RC2
RC: Graupner MX16 Hott with GR16
Telem.: 433 Mhz SiK
AUW: 2550 g
Log: here
Posts: 1
Participants: 1