@Michael_De_Leon wrote:
https://drive.google.com/open?id=1BEzd7yjOBSKd-xVlYXcYl1qChuOh9ibn
https://drive.google.com/open?id=1EO-2JvWrgjx-m5puxMjYF0nfOz6AHQlNEncoutered Multiple issue during this flight
-Compass error
-Airspeed and groundspeed
-Roll input was not responding during last approachIve transition to Q_loiter to stop the unit from flying away and returned safe. Just wanted to know what causes the issues. Thanks
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