@Raviv wrote:
Hi,
I encountered an interesting crash today.
Quadcopter running 3.4.2 on a pixhawk with zubax gps, idled all 4 motors in the air for no apparent reason.
The quad was in guided mode and fell from the sky.Reviewing the log showed all 4 motors going down to 1000 with no reason.
I suspect it has some thing to do with 3.4.2 since my other quads (2 of them with 3.3) fly perfectly with the same configuration.2016-11-27 14-27-43.bin (3.1 MB)
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