@zveruga wrote:
Hi.
I need help to explain strange copter's behavior.
While hovering in Loiter mode on 75m in air telemetry has lost, at the same time data logging is stopped and copter began to fall flat on his side.
I do full throttle on RC. On about 50m copter has reacted, leveled and began to slow down the fall. But it did not have time to full stop and landed (hard).
On log-file power not very clean and there is an assumption that there was a power drop below the critical value.
Question:
1. Is it possible that the controller rebooted in the air and after continued to fly? I do not re-Arm it.
2. Do you remember any cases when controller partially freezes (stops datalogging and telemetry output) but can react on RC sticks?
3. Can you guess another possible scenario for this behavior?
Copter: Big Octa, firmware 3.4.6, props 18", 6S LiPo
Posts: 5
Participants: 2