@Ekci wrote:
Hey, we have performed our first few tests of VTOL transition with 3.6 firmware. First AUTO mission was perfect (VTOL takeoff, few waypoints and VTOL land).
During second attempt (same mission) our horizontal motor just turned off few seconds after transition has started. RCOU.C3 just went to 1000. I've tried QRTL but I was behaving strangely so I landed using QHOVER.It's not a problem with motor or ESC, so what went wrong? Logs: https://www.dropbox.com/sh/1svs0v01da784p5/AAAvEPE6_OFF6VH6J_4RDotoa?dl=0
I can upload a footage from tail camera if needed (all motors are in frame).
Thank you for helping me and thanks for new firmware!
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